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Textiles wastewater treatment using anoxic filter bed and biological wriggle bed-ozone biological aerated filter
Authors:Fu Zhimin  Zhang Yugao  Wang Xiaojun
Institution:a Guangdong Esquel Textile Co., Ltd., 528500 FoShan, Guangdong Province, PR China
b College of Environmental Science and Engineering, South China University of Technology 510006, Guangzhou, Guangdong Province, PR China
Abstract:In this study, the performance of the anoxic filter bed and biological wriggle bed-ozone biological aerated filter (AFB-BWB-O3-BAF) process treating real textile dyeing wastewater was investigated. After more than 2 month process operation, the average effluent COD concentration of the AFB, BWB, O3-BAF were 704.8 mg/L, 294.6 mg/L and 128.8 mg/L, with HRT being 8.1-7.7 h, 9.2 h and 5.45 h, respectively. Results showed that the effluent COD concentration of the AFB decreased with new carriers added and the average removal COD efficiency was 20.2%. During operation conditions, HRT of the BWB and O3-BAF was increased, resulting in a decrease in the effluent COD concentration. However, on increasing the HRT, the COD reduction capability expressed by the unit carrier COD removal loading of the BWB reactor increased, while that of the O3-BAF reactor decreased. This study is a beneficial attempt to utilize the AFB-BWB-O3-BAF combine process for textile wastewater treatment.
Keywords:Textile wastewater  Biodegradation treatment  Ozone oxidation  Sulfate elimination
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